Forráskód Böngészése

iio: hudmidity: hdc100x: fix incorrect shifting and scaling

Shifting sensor data to the right 2 bits was incorrect and caused the
scaling values + offsets to be invalid.

Reported-by: Alison Schofield <amsfield22@gmail.com>
Signed-off-by: Matt Ranostay <mranostay@gmail.com>
Tested-by: Alison Schofield <amsfield22@gmail.com>
Cc: <Stable@vger.kernel.org>
Signed-off-by: Jonathan Cameron <jic23@kernel.org>
Matt Ranostay 9 éve
szülő
commit
94bef000f1
1 módosított fájl, 8 hozzáadás és 8 törlés
  1. 8 8
      drivers/iio/humidity/hdc100x.c

+ 8 - 8
drivers/iio/humidity/hdc100x.c

@@ -164,14 +164,14 @@ static int hdc100x_get_measurement(struct hdc100x_data *data,
 		dev_err(&client->dev, "cannot read high byte measurement");
 		return ret;
 	}
-	val = ret << 6;
+	val = ret << 8;
 
 	ret = i2c_smbus_read_byte(client);
 	if (ret < 0) {
 		dev_err(&client->dev, "cannot read low byte measurement");
 		return ret;
 	}
-	val |= ret >> 2;
+	val |= ret;
 
 	return val;
 }
@@ -212,17 +212,17 @@ static int hdc100x_read_raw(struct iio_dev *indio_dev,
 	case IIO_CHAN_INFO_SCALE:
 		if (chan->type == IIO_TEMP) {
 			*val = 165000;
-			*val2 = 65536 >> 2;
+			*val2 = 65536;
 			return IIO_VAL_FRACTIONAL;
 		} else {
-			*val = 0;
-			*val2 = 10000;
-			return IIO_VAL_INT_PLUS_MICRO;
+			*val = 100;
+			*val2 = 65536;
+			return IIO_VAL_FRACTIONAL;
 		}
 		break;
 	case IIO_CHAN_INFO_OFFSET:
-		*val = -3971;
-		*val2 = 879096;
+		*val = -15887;
+		*val2 = 515151;
 		return IIO_VAL_INT_PLUS_MICRO;
 	default:
 		return -EINVAL;