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ARM: dts: LogicPD Torpedo: Fix I2C1 pinmux

The pinmuxing was missing for I2C1 which was causing intermittent issues
with the PMIC which is connected to I2C1.  The bootloader did not quite
configure the I2C1 either, so when running at 2.6MHz, it was generating
errors at time.

This correctly sets the I2C1 pinmuxing so it can operate at 2.6MHz

Fixes: 687c27676151 ("ARM: dts: Add minimal support for LogicPD Torpedo
DM3730 devkit")

Signed-off-by: Adam Ford <aford173@gmail.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
Adam Ford 7 年之前
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當前提交
74402055a2
共有 1 個文件被更改,包括 8 次插入0 次删除
  1. 8 0
      arch/arm/boot/dts/logicpd-torpedo-som.dtsi

+ 8 - 0
arch/arm/boot/dts/logicpd-torpedo-som.dtsi

@@ -66,6 +66,8 @@
 };
 
 &i2c1 {
+	pinctrl-names = "default";
+	pinctrl-0 = <&i2c1_pins>;
 	clock-frequency = <2600000>;
 
 	twl: twl@48 {
@@ -136,6 +138,12 @@
 			OMAP3_CORE1_IOPAD(0x21b8, PIN_INPUT | MUX_MODE0)	/* hsusb0_data7.hsusb0_data7 */
 		>;
 	};
+	i2c1_pins: pinmux_i2c1_pins {
+		pinctrl-single,pins = <
+			OMAP3_CORE1_IOPAD(0x21ba, PIN_INPUT | MUX_MODE0)        /* i2c1_scl.i2c1_scl */
+			OMAP3_CORE1_IOPAD(0x21bc, PIN_INPUT | MUX_MODE0)        /* i2c1_sda.i2c1_sda */
+		>;
+	};
 };
 
 &uart2 {